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Heading COG Mismatch (E125/ACU400/EV-1/P70/I70)
06-12-17, 03:57 PM (This post was last modified: 06-12-17 03:59 PM by Chuck - Raymarine - Moderator.)
Post: #4
RE: Heading COG Mismatch (E125/ACU400/EV-1/P70/I70)
lwitty,

What was the maximum deviation detected by the Evolution autopilot? When was the autopilot installed? What version of software is presently installed within each of the autopilot components (MENU->SET-UP->DIAGNOSTICS-ABOUT PILOT)? Regarding the possibility that the problem may be resulting from integration with another device, please attach a system diagram (a photo of hand drawn diagram will suffice) identifying each device (including computers) and how each as been interfaced to the system.
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RE: Heading COG Mismatch (E125/ACU400/EV-1/P70/I70) - Chuck - Raymarine - Moderator - 06-12-17 03:57 PM

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